The project started with a call from Graham from
Bombala NSW enquiring about a 3-1/4 piston kit I had put together for a grey
Holden engine. He owns a restored FJ Holden and was wanting to repower it with
a hot grey and top it of with something unusual. I suggested a multi point EFI
and electronic ignition to which he agreed and away we went from there.
I had in stock a standard bore Canadian block (as the myth
goes). These blocks were believed to
have been able to be over-bored to 3-1/4" so to be sure we had the team at
Orger Engines in Bayswater, hot tank, crack test, pressure test and sonic test
the bore walls for thickness and core position, which is critical when
overboring an older engine to large sizes. It was determined that this block was
not suitable for our project. The lack of parent metal around the bore would
not support the deck surface leading to deck distortion and possible head
gasket I failure and overheating. I then provided three more blocks for
inspection and all failed. I had been warned I may have to go through as many
as 10 blocks to find one suitable, at around $300.00 a block we decided not to
worry. A 3-3/16" piston kit was purchased instead and our project was
under way.
Prior to the acid cleaning we removed all welch plugs and
scratched out the lower troughs of the water jackets to remove hard scale that
acid cleaning often does not remove. Removal of the main oil gallery plug at
the rear of the block and using a length of 5/ I 6' rod to tap out the front
oil gallery plug is also essential to cleanliness before we start. Don't forget
to refit this gallery plug on reassembly.
The first machining was to bore and hone the cylinders and
then to machine the deck. It required the removal of .015" to clean up and
another .015" to aid in compression gain. On the bottom end, in the past,
main bearing strengthening caps were bolted over the main caps. These are
becoming hard to get so we fitted a set of EJ caps which are much stronger than
the other models and then once again line-bored the main tunnels. The main bearings were then fitted and the ID
measured to calculate an accurate size to grind the crankshaft journals.
Below: The grey con
rods are robust and reliability can be assured by doing several simple mods.
Rod bolts from Mitsubishi four cylinder can be used, or they are also available
from ARP Fasteners.
The grey crankshaft has an inherent problem with breaking if
held in the high 5000 RPM zone. The ideal fix is to replace it with a similar
period Vauxhall six crank. This is an expensive job so I selected a crank that
had only shallow factory balance drillings in the counterweights which lessens
the interruption of the casting grain. Heat treatment or Tuff Triding is also
recommended. The flywheel was lightened
and a red motor style modern harmonic balancer was acquired to assist in smooth
running. Grinding the journals to undersize presents no problems when it comes
to strength as a competent grinder will grind in a large radius in the fillet
area that helps in retaining strength.
The grey con rods are very robust and reliability can be
assured by doing several simple modifications. Rod bolts from a Mitsubishi four
cylinder can be fitted, or they are also available from ARP Fasteners.
Polishing the side beams, shot peening all over and resizing makegthefobrig
nice tunnels will rods.
The was camshaft sent to Wade Cams in Oakleigh for
regrinding, it is important to check the distributor drive gear as they are
prone to wear, rendering the cam not serviceable. The grind selected was
usually used in speedway cars and is a little strong for smooth street use, but
as we were using electronic fuel injection this will help maintain high
manifold vacuum and lowdown driveability and a nice lumpy idle at the tailpipe. We fitted a billet steel timing gear supplied
by Motor Improvements in St Kilda and pressed it on with .006" clearance
to the thrust plate.
The bottom end was now ready for the final cleaning and
assembly. To assure no piston ring damage the bores should be scrubbed with a
course nylon brush and strong detergent to remove honing residue.
Once the crankshaft and number one piston were fitted, we then slid the camshaft in and set up the dial indicator and degree wheel to check our cam timing specs were correct. With only one piston in it is much smoother to turn the engine over to make accurate movement to read our specs.
GM recommend 006" backlash on the timing gear. With the gears in mesh I noticed there was no
backlash at all, which is a recipe for failure as the gears will grind
themselves away. We rotated the crank at 90° intervals and it was still tight, after scratching our
heads we realised that the line boring had closed the centreline dimension
between cam and crank, so we removed the cam, pressed the gear off and had the
gear teeth recut to give the required backlash and saved a disaster.
With the bottom end now assembled, we set about to
recondition the oil pump. The common
wear area is the end plate so we resurfaced it and on reassembly fitted a new
old stock kit that includes a new relief spring and plunger.
The cylinder head was supplied by the owner which he
purchased already built. It had been ported out and red motor valves fitted,
double valve spring kits are a little tough to find so standard V8 Holden
springs canbe used which will give around 80Ibs closed seat pressure and no
problems nbe used which will give around 80Ibs closed seat pressure and no
problems with bending pushrods. A standard thickness head is around 3.300"
thick, most heads can be machined down .100" to achieve a compression
ratio of around 8.00:1. There is a telltale casting mark on the gasket face of
around .060" deep that will give you a clue of previous machining.
Regularly on performance engines the head bolts are replaced
in favour of studs. I fitted ARP studs that come with ground hardened washers
and deep nuts in black oxide finish. On fitting the head gasket they can be
moved around a little so it was positioned so that the fire ring was concentric
with the top of the bore.The head was then fitted and torqued down using moly
lube under the washers and on the threads. A small problem is created when
fitting the side plate after heads and blocks are machined. The bolt holes into
the block must be elongated and the rear lower corner trimmed around the
distributor boss area to allow it to seal up. The rocker gear was reconditioned
as standard and the only modification was to screw a small self tapper into the
oil feed union bleed hole in the middle of the two rocker shafts.
Above: In the past,
main bearing strengthening caps were bolted over the main caps. These are hard
to get so we fitted a set of EJ caps which are much stronger than the other
models and then once again line-bored the main tunnels.
The engine was then sealed up and painted which led us onto
the next owner request of speed equipment with a difference. The distributor
building was handled by Dick O'Keefe from Performance Ignition Services in
Nunawading. He used a Ford style electronic body and custom made low resistance
spark Ieads. We supplied an original
drive gear and he machined the base and shaft to suit. It was then re-graphed
to suit the compression and fuel to be used.
The induction was to be the highlight of the project. When we first spoke I opened my big trap and
said that I had begun to assemble a multi-point fuel injection and needed an
engine to fit it to plus a reason to complete it. We started with my own cast throttle bodies
that were bored to I - I /2" and SU butterflies and shafts were fitted. I
then fitted spun alloy ram tubes to the intake side to keep it looking old
style. The computer was our next task. I
decided to use the Autronic system for several reasons, primarily the local
agent, David Baillie, has been working with this system for years and works
closely with me in my workshop using the Autronic air/fuel ratio computer to
cure many street and race car problems we are faced with. They are also an
Australian company. With the help of Richard Aubit the owner and designer of
these systems, we fitted 5.7 litre Commodore injectors on a common fuel rail, a
Commodore fuel pump and an adjustable fuel pressure regulator.
These projects always present problems in getting them up
and running so we enlisted the help of Danny Selva from Selva Racing Poewr Dyno
services to help make the jigs and set the engine up on his dynometer. David Baillie pre-set the computer to a general
start mode, we spun in over to get up oil pressure, hit the start button and it
fired into life. I fitted a weld-in bung
to the header pipe and had the oxygen sensor screwed in so that we could accurately
make adjustments as we loaded the engine
up with the fuel it required through the RPM range. These systems aslo have a cold start
capability inbuilt that are also adjustable.
After a day in the dyno room we were happy with the engine and
it was ready to be fitted to the car.
The owner did the fit off and David and I drove across to Bombala to do
the final on road setup with the portable ait/fuel ratio meter fitted in the exhaust
system. The vacuum characteristics
changed a little with the car weight so it’s essential to complete the final
adjustments while in the car.
Article from Street Rodding magazine by Malcom Chruch.
Hi, with the "Canadian"block, how are they identified? Is it the different logo cast into the side?
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